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The Project: The K1 group are responsible for the general upkeep of the locomotive. They look after winter maintenance and any improvements to its operation. |
K1 Working Parties
Volunteers will be welcome at the working parties so in the first instance please contact any of those listed on the Group's details page. More details and advice on equipment is on the 'Volunteering with K1' page. Next Working Party to be advised. April 21st/22nd K1 Working Party Report.. The usual two of the team were on site, John Startin and Nobby Clark, Nobby having travelled over in the early Saturday morning from Cambridge. K1 has a huge following once again illustrated at this Working Party. An American from New Jersey came to see K1, preferably in steam. He has been all over the world including the Dundas Tramway in Tasmania and has a strong interest in the Garratt locomotive type not adopted in the States. We did all that was possible by way of a tour of the engine. With K1 in the back of the carriage shed we set about the two chosen objectives, the floor and the steam feed route for the generator. With the centre section of the
floor already completed we repaired the
existing battens, an additional batten added across the front, and two
more behind the rising sections to stop them moving outwards.
We have sent three sets of
suggestions to the Railway Workshops for machining the pivot brass
casting that has replaced the Delrin liner. The original base
has tell-tale marks as to where the lubrication grooves are in the base
and on the spigot. It also shows a distinct lack of
lubrication. ![]()
At the time of writing the next two working parties in May & June may not go ahead as John is not available for both, and Nobby not in June. We will advise via this website of any changes.
March 19/20th K1 Working Party
Report. John Startin writes. My thanks to Nobby Clark for his help and company. Nobby is a stalwart volunteer traveling over from Cambridge regularly since 2000 to work on K1 as well as volunteering with the East Anglia Group. With just the two of us a great deal was not going to be accomplished. We did have another look at the generator steam pipe run which will have an awkward run to reach the supply point. This must be done ahead of fixing the cab floor battens and further work on the floor. We had been specifically asked by Tony to trial fit the new ball joint and our attention was applied largely to that alone. The ball joint assembly was
waiting for us at Dinas! Further evidence for concern
over these is that the flanges securing the pipe to the cylinders are
splitting the weld to the pipe on both sides. (Andy Shaw spotted this
while having a look at the Ball Joint.) These pipes have to
come
down anyway making the repair a simple matter. With the parts
removed the new casing was positioned to explore its fit and to
identify problems that might arise. Our attention then turned
to
the problem of securing the ball pipe to the J pipe. The
existing
arrangement might just have fitted but it does not. The use
of
four springs instead of three would have eliminated this but meant the
cover would then not be the same and the springs too would be different
from the later engines. I considered that the commonality of
parts was more important. The three stud arrangement is
easier
for maintenance as the access to the springs is easier, they can be
removed in situ, the top two cannot as it is. The clamps used
have remained the same from K1 right through to the NGG16s.
The
pipe is much shorter on K1 hence the problem. Nobby and I
considered several ideas before finding a suitable one and had the
spring studs been right required only that they be shortened and
castellated nuts be used to secure them.
A different
design of flange coupling has been devised to be drawn up to be
made. Various gasket material has to be researched for
refitting
of the pipes, etc. And the 'Y' pipes and others have to be
removed before the main re-assembly with new gaskets. January 21/22nd 2012 K1 Working Party Report.
John Startin reports: The
weekend’s work objective was to remove the pivot base, assess the
repair required and fit a temporary pivot base, without dismantling a
lot of the
motion, etc, so that K1 could be moved around or from the
running shed without hindering other loco’ work. Access to lift the
engine under the ends of the cross member required the expansion links
to be
disconnected and laid back out of the way. The reversing rod
required releasing and to do this the hind expansion links were blocked
up, balancing the weight of the front gear. This was done without the
need to move
the power unit out from under the frames. After lunch on
the Saturday the lift was made. The pivot bolts which are “fitted”, had
to be driven out and considerable careful leverage applied to the base
as it has lugs around the cross member. The temporary pivot base was
then offered up and once shown to fit, Sunday was spent cleaning up the
nuts and bolts ready for re-assembly, looking at steam leaks and the
pivot on the NGG16 for comparison. The Delrin liner in K1’s pivot base
had to be cut in situ to release it. It is in two parts - most of the
base as one, and the edge and sides as a second piece. Lack of grease
caused by the grease channels in the upper face being partly blocked as
the Delrin became deformed. Compared with the NGG16 brass base liner,
it is the same thickness as K1’s but the question now is how to make
the base and edge by fabrication or as a casting. The edge will have to
The high-pressure steam pipes to
the cylinders have given way twice now, once on each side, so a
detailed look and measurements have revealed errors. The choice of
gasket material may relieve some of the problems, as on the NG15’s it
is round section copper, that does not require chiseling out unlike
flat section. This is difficult to fit on the Y pipe used on K1, as
this requires the exhaust manifolds to be removed. The steam supply
pipes have been a cause of concern right from the beginning, as the
bends from the Y pipe to the cylinders have to be fitted first. The
pipe from the Y pipe to the return U bend onto the ball joint has
always been awkward to fit. It is tight against the frame stretcher.
Careful attention to the drawing shows the assembly of the pipe, return
bend and ball joint is not as it should be. The design allows the pipes
and ball joint to be fitted to an auxiliary plate that is in turn
retained to the rear stretcher. The auxiliary plate is too thick and
the steam pipe from the Y pipe to the U bend is too long, hence a
mis-alignment. The proper length for the steam pipe may For the rescheduled working party on April 21st/22nd, the route for the steam supply to the generator was examined. Two steam pipes for the sanding and steam brakes run inside the frame and these have been repositioned upwards at a joint to give the supply pipe a straighter run. One of these pipes has an extra section inside the cab now not required with the removal of the oil firing. Repositioning of these pipes will tidy up inside the cab and perhaps allow a much simpler run from the generator supply. And the new cab floor may well get fitted up with battens, etc. Autumn 2011 Working
Parties ReportWorking parties on K1 this Autumn have been tackling jobs that hopefully will remedy reliability issues that have prevented the locomotive being used on shorter service trains. A problem has arisen with the front engine unit pivot and it was planned on Nov 19/20th to lift the main frame so that the pivot bearing could be reached and removed and replaced temporarily with an ambulance pivot made out of a
steel frame and wood core bearing so that K1 could be moved slowly
within the running shed area. With access difficult within the confines
of the engine frames it was decided to remove the front tank, which is
not a huge task in itself as the fixings and water connection are quite
quickly released. And as can be seen from the photo, the tank can be
slung off by a large fork lift with the appropriate slings. The
close
up of the bearing shows the inner liner suffering from distortion and
it will have to be replaced with a new brass bearing liner, assuming
there are no other problems. The casting itself looks o.k, so hopefully
that will cure the clanking and some of the oscillation from the front
engine unit. Work will proceed on removing this casting now access is
better. The
centre section of cab floor has been made,
and offered-up
into position to assess the remainder of the timber that will be
re-used. Extra battens will support the new floor that is tied together
to prevent coal dust building up on the steel footplate beneath, and
drifting down over the lubrication pipes beneath. The original centre
section had been altered over the years with oil firing equipment
removed and alterations to the injector drains creating a battered
section of woodwork. A steel plate will be placed in front of the fire
hole door to run crossways to help with protecting that area of wood.![]() The previous working party in October prepared K1's boiler for inspection and wash down, removed and measured the flooring. Also the team of John, Nobby, Martin and Andy did preparatory work with the new ball joint castings, and investigated the reported steam leak areas for visual signs. We were helped by Andy Williamson and Andie Shaw with shunting and lifting, etc. Working Party reports for Feb 5/6th & Mar 5/6th 2011 A considerable effort has been achieved resetting the valve timing on K1 with an excellent improvement in performance. Thanks are due to Llyr ap Iolo for his work on this. Following on from K1's first few days of service in 2011, the team have tackled lubrication issues, both greasing and oiling motion parts, assessing pipes for chafing, and replacing trimmings. The axleboxes flexible pipes were cleaned and inspected with notes for replacements made. Some tidying of cab fittings, including a replacement soft cover for the fireman's seat, and assessing the wooden cab floor for partial replacement and repair. The redundant fireman's side injector drain piper was removed so that a steam pipe can be run to the turbo generator. Work continues on these electrics and tests have been made with led's (light emitting diodes) for cab and water gauge illumination. We know now the type of illumination to use, but we have to encompass those led's used on the water gauges in heat resistant shrouds with heat resistant wiring. The next regular working parties will be held in 2012, to be advised, and the regular K1 AGM will take place on the same weekend as the WHRS AGM, a flyer and e-notice will be sent later in the year. We had a team of 5 on Saturday and 3 on Sunday working on K1 in the carriage shed at Dinas, all in glorious sunny weather. Work continued on the motion parts, general refurbishment of cab fittings such as the seats, and checking underneath the locomotive for lubrication and steam leaks. K1 is now in service after again after much work by the volunteers and workshop staff throughout the Spring and early Summer of this year. Refurbishing the interior of the cab, such as a new fireman's seat cushion, handbrake gaiter, leather window straps, etc, have been fitted. A new stainless steel blast-pipe has been fabricated and fitted, the boiler pressure has been reduced to 190 psi, pipe-work and motion dealt with. This is quite a long list but more details are in the K1 2010 Summer Newsletter published for members. If you would like to be kept informed of K1's progress then why not joing the K1 group. Details on the membership page.
K1 working party report for Feb 13/14th 2010. They had a productive weekend, ( 7 members on Saturday, 6 on Sunday) and completed the following jobs:-Most boiler tubes were rodded through, apart from the two on the right hand side at the bottom, that defied getting the brush in a couple of feet in the first tube and about half way for the second tube. At least a dozen tubes were blocked, mainly behind the blast pipe. The team removed, cleaned and refitted all 4 sanding pipes and nozzles. They found that the fireman's side rear pipe and nozzle was not standard and is missing a locating spigot in the flange which might be causing a sand trap. Front drivers side stone guard refitted & the fireman's cab handrail tightened. The low pressure engine crosshead and the connecting rod, union link and other motion parts were removed. But the other associated motion parts were put back so K1 can be moved. The two low pressure engine snifting valves were removed and lapped in. One gasket had clearly blown out, and so these require remaking at or before the next working party. They also investigated the low pressure right hand side coupling rod little end bush which appears to be loose. A more detailed report on this will follow. Cab gauges were fitted up but not connected. The big end and crosshead oil pots were removed to be used as patterns for replacements. Early 2010 2010 did not get off to a good start with the working parties as the first one in January was canceled due to the bad weather that swept the UK at that time. The next one was therefore held on February 13th & 14th. Note: More details about earlier work on the locomotive are to be found on the WHR Project's K1 pages. |